Tektronix 545
                  OscilloscopeDate of introduction: 1955

Type: Cathode Ray Oscilloscope

Bandwidth: up to 33MHz (plugin-dependent)

Power requirements: 230V, 535 Watts (5354C plug-in)

Dimensions: Height: 42.5cm (16.75"), Width: 33cm (13"), Depth: 61cm (24")

Weight: 32kg (65lbs)

S/N:



Story:

In autumn 2016, I bought this oscilloscope on ebay for 130 Euros. I was very tempted to get it, as the 545 oscilloscope does not contain transistors, yet. It's all-tube technology. I got very interested in starting to work with tube technology during a repair weekend I did with Prof. Bernd Ulmann. There, we tried to repair a Tektronix 547 oscilloscope, which uses a mixture of tubes and transistors.
The seller of the 545 'scope was located nearby my place. Thus, a pick-up was very convenient.  This unit came with a CA-plug-in and a special trolley which can hold two more plug-ins. He told me that I got this oscilloscope from the Physics Department of the Karlsruhe University of Technology when the oscilloscope was decomissioned there in the early 1990's. He had the scope since then in his house, but never used it. Additionally, he said that he made a small test by turning it on, but the CRT beam became not visible. That meant that I would have to repair it - challenge accepted ! :)

It follows a little blog of my repairing and restoration project that began in March 2017:

First, I connected the 'scope to a variac and ramped up the voltage to 230 volts.  I made to observations:

    1. The CRT beam only became visible when the trigger was set to "external trigger".
    2. After 15 minutes, strange noises started to appear. Probably one or more capacitors started to suffer from the heat due to leakage-related issues.

 It was time to get the service guide and verify the proper operation of the power supply circuit. I was impressed that it provides five different high voltages! First, the resistances for the five voltage rails need to be checked according to table 2.1 on page 37:

-150V to Gnd: 3kOhm or more: 3.2kOhm: ok

+100V to Gnd: 5KOhm or more: 10.9kOh: ok

225V to Gnd: 5KOhm or more:  5kOhm: ok

+350V to Gnd: 10KOhm or more: 18kOhm ok

+500V to Gnd: 25KOhm or more: 38kOhm: ok

Important is to not forget to insert a plug-in as when measuring the resistance of the 100V-Gnd rail, as stated in the service guide. This supply rail is amongst others used for the plug-ins! I forgot to plug the plug-in back into the 'scope and was fooling around for quite a while before realizing that the plug-in had to be in!

The next step was to test the relay which went well. Here, a dual-trace plug-in unit is needed and I was happy that it was part of the plug-ins that came with the oscilloscope.

Next, I measured the supply voltages with a voltmeter at a position at the bottom of the 'scope as advised by the service guide. The voltages are required to be within a tolerance of 2%.

545
              PSU voltage measurements
The five voltages can be measured at the lines that are between the resistors (right side of picture).




 Voltage rail:

-150V

+100V

+225V

+350V

+500V

Measured voltage:

-148V -> ok

96.2V -> too low

172 -> too low

362 -> too high

510V -> ok




The 500V rail is the result of inverting and adding the 150V rail to the 350V rail. Three voltage rails had voltages that were not within the required tolerance. In case of the 225V rail being too low, the service guide recommended to change the tube V748 (of type 6080) and to check the 0.01uF capacitors C763 and C770. First, I had to get spare tubes! So I checked ebay and got a Thomson new-old-stock (NOS) replacement tube. The replacement led to the +225V rail being in the required tolerance! The +100V and +350V rails still were out of tolerance, though. In that case, the tube V742 was to verify.  The service guide recommended to check for that tube of type 6AU6. Interestingly, this tube was probably changed in the past already, as there was a Lorenz EF94 tube seated in the V742 socket.
Again with the help of ebay, I bought some unused tubes from GE that were certified and tested by Tektronix (PN: 157005900)! Replacing V742 helped to bring the two voltages back into the required tolerance range.
Below is the summary of the measured voltages.

 Voltage rail:

-150V

+100V

+225V

+350V

+500V

Initial measurement:

-148V -> ok

96.2V -> too low

172V ->too low

362V -> too high

510V -> ok

after V748 change:

-149.2V ->ok

134.4V -> too high

225.2V -> ok

365V -> too high

496V -> ok

after V742 change:

-149.4V -> ok

99.5V -> ok

225.4V -> ok

347.2V -> ok

496V -> ok

 


V748 tube replacement
Left tube: Thomson Replacement, right tube: defective Valvo tube.


V742 replacement
Left tube: defective Lorenz EF94, right tube: GE replacement tube which was certified by Tektronix for use in their equipment.


New tubes in place
The two new replacement tubes in place: The large 6080WA and to its right the GE EF94 tube.

The two new tubes look shiny compared to their neibhours. I decided not to clean the working tubes that are in place since I am afraid that the tube type markings may be cleaned off, too.




Resistor replacement:

While carefully doing a visual inspection of the components, I stepped over the resistor shown in the picture below:

broken resistor

 
During desoldering, it turned out that it was broken in two halves! As the color code was not visible anymore, I tracked the resistor down in the schematics (R1007) and replaced it.

Capacitor replacements:

While reading experiences done with other Tektronix 500-series restoration projects, there were contradictory statements and discussions related to paper-tape-based capacitors from the 1950s. They seem to become "leaky" over time and some people wrote that it would be best to replace them all. Others state that they did not experience issues with this capacitor type. These capacitors seem to be known as "Black Beauties" or "Bumblebees". As I was in the processing of repairing & restauring the scope, I decided to replace them all except for a few high-voltage capacitors. Regarding the latter, the problem was that I could not locate a supplier that sells these per piece, they usually are sold at minimum amounts of 500 pieces or more.

paper-tape-based
              capacitors

Desoldered paper-tape-based capacitors


capacitor replacement
The yellow-collored capacitors are the new ones.

capacitor replacement
Close-up of the replaced capacitors. One may spot that the cap at the front has a melted package corner. During soldering, I accidentally hit it with my soldering iron...

In addition to the paper-tape-based capacitors, one of the large electrolytic caps with aluminium housing was leaking. Since I dediced to keep the look and feel of this large type next to his "neighbours", I unsoldered this capacitor, cut him open and removed its content. I placed its capacity of 125 uF with three modern electrolytic caps: 100uF, 10uF and 15uF and connected them in parallel to obtain the same
capacitance the old one had.

power supply
                  capacitors
The right one of the two black-coloured capacitors was showing leackage on the bottom side and had to be replaced.

 The three caps were mounted on the aluminium socket of the former capacitor and were covered by the original black paper cover so that the transformation using new components is kept secret :) This preserves the original look of the capacitor section. The work required was one and a half hours to get this done - and it's totally worth!


three new caps
                  sitting on the socket of the original cap
The two smaller caps had to be stacked to make everything fit into the socket of the former capacitor.


three new caps
                  sitting on the socket of the original cap
Nice comparison of the sizes between the cap technology from the 1950s and technology from the 2010s
 

fixed large cap and
                  two new tubes
  Once the work was done, the black paper cover was slided back on the aluminium socket to preserve the original looks.


Then, I slowly brought up the mains voltage up to 230V using a variac and the main secondary voltages of the power supply were within expected tolerances  as given in the manual.
I could thus proceed with the testing procedures as described by Tek.
The PSU output voltage ripples where checked using a working Tek 5403 oscilloscope and turned out to be within the specification.

As a next step, I decided to reajust the precision "-150V rail" to have it precisely set from -149.3V to -150.0V. Since all other output voltages are derived from that rail, I had to check all other voltages again:

 

 nominal voltages

-150V

+100V

+225V

+350V

+500V

Voltage measured DC after readjustment

-150.0V

99.8V

225.8V

348.5V

499V



  Following the course of actions described in the manual, I continued with a look at the function of the calibrator circuit which is supposed to deliver a rectangular signal at a fixed frequency. Here, the voltages were within the tolerances as stated in chap. 3 of the Tek service manual.

Chap. 4 deals with the high-voltage section of the oscilloscope. the task is verify, if the output voltage is around -1400V. Using a high-voltage probe Tektronix P6015 on the 5403 oscilloscope, I verified that the high voltages were within tolerance. Since very high voltages are implied, such works need to be done with particularly much precausion. Never do this in a hurry, double-check everything before starting with measurements!!!
Since the PSU high voltage outpus was fine, I continued with section 4.1.2 to verify the cathode supply regulation. The proper function can be visually checked by setting all scpoe settings according the the Tek guide. If things are in working order, a bright, defocused trace should appear. However, in my case, noting appeared on the tube!



According to the recommendations of Tek (chap. 4.1.4), it was then time to connect the calibrator output to one of the inputs of the plug-in that I got with the 545 scope. After playing a bit with the vertical and horizontal deflection settings, I figured out that the scope only showed a signal within the left half of the cathode ray tube. The vertical shifting and scaling, however, worked well.

Signal only spanning
                  over the left half of the tube
The calibration signal was only visible on the left side of the screen, no matter the horizontal deflection settings chosen.

Thus, I had a look at the beam position test function.  There was no way of moving the beam to the right side of the CRT. Vertical positioning works properly and vertical position indicators, too. So a problem must still reside somewhere in the horizontal deflection electronics, i.e., the sweep amplifier.

In order to verify the voltages of the horizontal deflection plates, I followed a description in the service manual in chap. 5.1.2., where the external sweeping setting and the magnifier x5 should be set in order to only obtain a centered spot on the CRT.
The right plate's voltage was 180V whereas the left plate was at 164V, which were both far from 310V to GND as stated in the guide. Moreover, the horiztonal indicator lights do not behave as expected, when turning horizontal position to left and right. Set to right position, the right light indicator stayed off, while on left position, the left turned on while the right one remained on, too, which is not the expected behaviour.
These indicators are supposed to indicate to which side the beam is deflected when it's outside of the visible tube area.

So I started checking resistors and some caps within the sweep amplifier. The result was that one resistor was electrically broken in terms of an open circuit (no electrical connection between its terminals) and two further resistors were far out regarding their their allowed resistance tolerances.
The resistors were the following ones:

  • R286 (mita plate, 6k & 30k resistors, 5W, +1% tolerance)  open regarding 30kOhm terminal
  • R267 (2.2kOhm, 1W, 10%) measures a very low value of 1.4kOhm -> out of spec
  • R292(470kOhm, 0.5W, 10%) measures low value of 390kOhm -> out of spec


The Mita plate type resistor is a specially made one with very low tolerance and integrates two resistors of which the 30kOhm section is "open". Here, I decided to leave the component in place regarding the 6kOhm section and replace the 30kOhm resistance by ordering two 15k resistors with low tolerance and solder them in series.

Special Mita
                  plate-type resistor
On the front: The rectangular Mita plate-type resistor, which seems to be a custom component with non-typical resistor values and low tolerances.


Special Mita
                  plate-type resistor
Close to the the rectangular Mita plate-type resistor are located two new black resistors that replace the 30KOhm section broken in that plate resistor.


Two new resistors
                  replace the ones that where out of tolerances
The two resistors that showed resistance values far off the allowed tolerance where replaced by new ones.




After their replacement, the main sweep worked fine and still does.

In order to complete the restauration works, I replaced all remaining paper-based capacitors of the device which turned out to be a lot of work. Often, these caps are very difficult to reach out to and to replace when they are located either under other components or at potentiometer that are behind the faceplate of the oscilloscope.

The final result: Connecting the calibration output to the scope channel input led to the following expected trace:
Expected rectangular
                  signal as provided by the calibration circuit
Expected rectangular signal as provided by the calibration circuit. The scope is working fine again!






In summary, with the help of the fantastically written and detailled service manual from Tektronix, fixing this wonderful oscilloscope was not difficult and it is ready to be used when I measurements for low-bandwidth applications are of importance, especially during cold winter days since 500 Watts of energy dissipation really help to heat up my workshop room.